Aircraft is on ground for 30 seconds and the aileron trim is not correctly configured for take-off.
Aircraft is on ground for 30 seconds and the rudder trim is not correctly configured for take-off.
Aircraft is on ground and the stabilizer trim is not correctly configured for take-off.
Flight spoilers are deployed below 500ft (not on ground) and/or the throttles are above idle (not on ground).
Roll spoiler switch is set to OFF and the roll disconnect switch is not set to disconnect.
A fault that causes the loss of redundancy has occurred in the spoiler system but does not affect spoiler operation.
There is a small malfunction in the flap system which does not stop the operation of the flaps.
A minor failure that causes the loss of redundancy has occurred in the rudder limiter system.
A fault that causes the loss of redundancy has occurred in the spoiler system but does not affect spoiler operation.
SPC has sensed a fault and has reverted to a default flap settings of 30 degrees.
Roll spoiler switch is set to OFF and the roll disconnect switch is set to disconnect.
MSW on one or the other control wheel has been pushed for less than 10 seconds or the pusher has been inhibited by the STALL PUSHER PBA.
