07/19/19
Message Overview:
| DDG Reference: | 28-21-05 |
| Pilot Action (QRH): | FUEL 09-29 |
| System Description: | 28-21-00 |
| Schematic Diagram: | 28-21-00 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Wiring Diagram: | 28-21-00 [ Global Express ] [ G5000 ] [ Global XRS ] |
Fault Description:
The left auxiliary (DC) pump is failed. The wing transfer function, from the failed side, is not available.
Possible Causes:
- Throttle Quadrant Assembly (TQA) (AP41) L Engine RUN switch (1S1)
- Fuel Management Quantity and Gauging Computer (FMQGC) (A47) racking
- Left DC Auxiliary Pump (B10)
- Left DC Auxiliary Pump Pressure Switch (S11)
- Associated Wiring
Troubleshooting Tips:
Advisory Wire/Service Bulletin:
- AW700-28-0368 - No Fault Found initiative: Fuel Management and Quantity Gauging Computer (FMQGC)
- AW700-28-0469 - Fuel Management and Quantity Gauging Computer Tray Connector Inspection
Forum Articles/Infoservice/Newsletter: None
NOTE: If the Left Primary AC pumps and the Left DC Aux pumps are showing inoperative after engine shutdown, go to Troubleshooting Recommendations step 2.
Quick Links:
| Access to CAIMS Active Faults | AMM 45-45-00-970-802 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Removal of the FMQGC | AMM 28-41-01-000-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Installation of the FMQGC | AMM 28-41-01-400-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Removal of the Throttle Quadrant | AMM 76-10-01-000-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Installation of the Throttle Quadrant | AMM 76-10-01-400-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
Troubleshooting Recommendations:
- Access CAIMS Active Faults and select fault message from menu below:
- If the left primary AC pumps and the left DC Aux Pumps are showing inoperative after engine shutdown, continue with next step.
- With the LH FUEL CUTOFF switch in the OFF position, check for continuity to ground between FMQGC connector A47AP1 pin H12 and ground.
- If there is no continuity, continue with next step.
- If there is continuity, go to step 7.
- On the TQA, check for continuity of the LH FUEL CUTOFF switch (1S1) between connector A41J2 pins 38 and 46.
- If there is continuity, continue with next step.
- If there is no continuity, replace the TQA.
- Check for continuity between connector A41P2 pin 38 and airframe ground.
- If there is no continuity, check the ground stud or repair defective wiring as required.
- If there is continuity, continue with next step.
- Perform wiring checks between the FMQGC and the left Engine Fuel Cut-off switch and repair as required.
- Remove the FMQGC and re-rack the unit fully and perform a re-test of the system.
- Do close out.