10/03/19
Message Overview:
Fault Message:
R CH B AIRCRAFT POWER LOST MA
Fault Code:
7327329RBR
Associated CAS:
| Reporting LRU: | Right Engine Electronic Controller (EEC) |
| System Description: | 73-20-00 |
| Schematic Diagram: | 76-10-00 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Wiring Diagram: | 71-50-01 [ Global Express ] [ G5000 ] [ Global XRS ] |
Fault Description:
This message is set when there is a failure of the aircraft 28 VDC power supply to channel B of the Engine Electronic Controller (EEC). The 28 VDC is supplied by the aircraft BATT BUS. These circuits are monitored by the Full-Authority Digital Engine-Controller (FADEC) when power is applied or the engine is started.
Possible Causes:
- Secondary Power Distribution Assembly (SPDA) 1 (A13)
- Right Engine Electronic Controller (EEC)
- Associated Wiring
Troubleshooting Tips:
Advisory Wire/Service Bulletin: None
Forum Articles/Infoservice/Newsletter: None
Quick Links:
| Engine Safety Precautions | AMM 71-00-00-910-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Opening of the Cowls | AMM 71-10-00-010-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Closing of the Cowls | AMM 71-10-00-410-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Visual Check of the Engine Controlling System | AMM 73-20-00-210-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Deactivation of the Thrust Reverser (for Maintenance) | AMM 78-30-00-040-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Activation of the Thrust Reverser (for Maintenance) | AMM 78-30-00-440-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Removal of the Engine Electronic Controller (EEC) | EMM 73-21-01-000-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Installation of the Engine Electronic Controller (EEC) | EMM 73-21-01-400-801 [ Global Express ] [ G5000 ] [ Global XRS ] |
| Wire Repair - Maintenance Practices - ALL | SPM 20-12-10-02 [ Global Express ] [ G5000 ] [ Global XRS ] |
Troubleshooting Recommendations:
- Perform troubleshooting for BATT BUS.
- If BATT BUS is not satisfactory, repair as required and do close out.
- If BATT BUS is satisfactory, continue with next step.
- Perform wiring checks between P1048 and 2PB4.
- If wiring checks are not good, repair defective wiring as required and do close out.
- If wiring checks are good, continue with next step.
- Replace Right EEC.
- Do close out.